If you need assistance, please send an email to forum at 4hv dot org. To ensure your email is not marked as spam, please include the phrase "4hv help" in the subject line. You can also find assistance via IRC, at irc.shadowworld.net, room #hvcomm.
Support 4hv.org!
Donate:
4hv.org is hosted on a dedicated server. Unfortunately, this server costs and we rely on the help of site members to keep 4hv.org running. Please consider donating. We will place your name on the thanks list and you'll be helping to keep 4hv.org alive and free for everyone. Members whose names appear in red bold have donated recently. Green bold denotes those who have recently donated to keep the server carbon neutral.
Special Thanks To:
Aaron Holmes
Aaron Wheeler
Adam Horden
Alan Scrimgeour
Andre
Andrew Haynes
Anonymous000
asabase
Austin Weil
barney
Barry
Bert Hickman
Bill Kukowski
Blitzorn
Brandon Paradelas
Bruce Bowling
BubeeMike
Byong Park
Cesiumsponge
Chris F.
Chris Hooper
Corey Worthington
Derek Woodroffe
Dalus
Dan Strother
Daniel Davis
Daniel Uhrenholt
datasheetarchive
Dave Billington
Dave Marshall
David F.
Dennis Rogers
drelectrix
Dr. John Gudenas
Dr. Spark
E.TexasTesla
eastvoltresearch
Eirik Taylor
Erik Dyakov
Erlend^SE
Finn Hammer
Firebug24k
GalliumMan
Gary Peterson
George Slade
GhostNull
Gordon Mcknight
Graham Armitage
Grant
GreySoul
Henry H
IamSmooth
In memory of Leo Powning
Jacob Cash
James Howells
James Pawson
Jeff Greenfield
Jeff Thomas
Jesse Frost
Jim Mitchell
jlr134
Joe Mastroianni
John Forcina
John Oberg
John Willcutt
Jon Newcomb
klugesmith
Leslie Wright
Lutz Hoffman
Mads Barnkob
Martin King
Mats Karlsson
Matt Gibson
Matthew Guidry
mbd
Michael D'Angelo
Mikkel
mileswaldron
mister_rf
Neil Foster
Nick de Smith
Nick Soroka
nicklenorp
Nik
Norman Stanley
Patrick Coleman
Paul Brodie
Paul Jordan
Paul Montgomery
Ped
Peter Krogen
Peter Terren
PhilGood
Richard Feldman
Robert Bush
Royce Bailey
Scott Fusare
Scott Newman
smiffy
Stella
Steven Busic
Steve Conner
Steve Jones
Steve Ward
Sulaiman
Thomas Coyle
Thomas A. Wallace
Thomas W
Timo
Torch
Ulf Jonsson
vasil
Vaxian
vladi mazzilli
wastehl
Weston
William Kim
William N.
William Stehl
Wesley Venis
The aforementioned have contributed financially to the continuing triumph of 4hv.org. They are deserving of my most heartfelt thanks.
Registered Member #1538
Joined: Thu Jun 12 2008, 07:28PM
Location: Bonn, Germany
Posts: 28
Hello everybody
Recently I ran into another problem with my DRSSTC. I tried some things to get rid of it, but nothing worked out. Now I’m somewhat stumped. Hopefully somebody can give me a useful hint. Just to give you a general idea: I use a circuit similar to Steve Ward’s, described here.
My problem is the following: The IGBT’s gate voltage dose not come to zero and remains zero after the ON-Time has past. Instead, when the driver chips enable pins go low, the gate voltage starts a damped oscillation. It passes through zero and reaches about 12V again, before it stays lower than the IGBT’s V_threshold. You can see it here:
IGBT’s gate voltage, 60V peak-peak, ~170kHz
This little overshoot at the end turns the IGBT on again. Here is a picture of the bridge output voltage, switching into a resistive load.
Output, ~50V peak-peak, “High†for about 3us in this picture (170 kHz)
You see that the lower IGBT is turned on for about 250ns by this unwanted overshoot. In my setup it would have to turn of about 2/3 * I_peak after this because there is already about 250ns delay between the zero crossing of the primary current and the “first†switching transition.
To clean up the gate signal, I tried to use short connections between the GDT and the IGBT, I tried different GDT designs, and I added up to 20 Ohm in series with the gate. Nothing worked. What else might be the reason? Or maybe it doesn’t matter that much? Dose anybody have an idea what else I could try?
Registered Member #146
Joined: Sun Feb 12 2006, 04:21AM
Location: Austin Tx
Posts: 1055
To fix that oscillation, i put a 10-50 ohm resistor in parallel with the DC blocking capacitor on the primary side of the driver. Try it and see if it fixes it for you, i had the exact same problem in the past.
Registered Member #1538
Joined: Thu Jun 12 2008, 07:28PM
Location: Bonn, Germany
Posts: 28
I tried 10 Ohm parallel to the DC blocking cap, but it doesn’t change anything. But maybe it’s because I used a film/foil type cap for this purpose. I did this because the elko’s ESR limited the maximum current and therefore the gate voltage rise time before. I will try to step back to an elko now. Anyhow, it seems you had the right idea: I made a picture of the voltage across the DC blocking cap (trace 1).
The lower trace is the gate voltage
Obviously there is a lot of ringing over the cap, too. I found this ringing to be exactly synchronous with the gate voltage overshoot.
My circuit is, more or less, the one Steve Ward uses. =>klick<=
Registered Member #1232
Joined: Wed Jan 16 2008, 10:53PM
Location: Doon tha Toon!
Posts: 881
As Dr Conner said, 6 turns is likely too few for 170kHz, depending on the Spec Ind (Al) for that core. I'd aim for about 15 turns on each winding on a high-permeability MnZn ferrite core.
I would also use a 1uF electrolytic in parallel with your film/foil DC blocking capacitor if it is less than 220nF. The suggested resistor across the DC blocking cap is also a wise addition is pulsed applications. This damps the transient response of the low-frequency resonance between the magnetising inductance and the DC blocking cap. Although that is not the problem here.
Also make sure you have a 100nF ceramic and at least 10uF electrolytic (or tant) in parallel across the supply rails right at each gate drive IC. This is important and often overlooked. When the drive IC switches on and tries to charge a power device's gate, this charge has to come from somewhere. It is best to provide a local store of charge close to the gate drive IC otherwise the local supply rail will sag and bounce due to inductance. This could possibly be causing your problem here.
Registered Member #30
Joined: Fri Feb 03 2006, 10:52AM
Location: Glasgow, Scotland
Posts: 6706
That's true. I stick a 330uF low-ESR electrolytic right on the supply pins of each gate drive chip. I used to use 0.1uF ceramics in parallel with those, but I quit and it didn't seem to make much of a difference. (I chose 330uF because I had a load of them that I bought for something else.)
I also used 4uF worth of DC block caps with a 10 ohm resistor across them.
My gate pulses looked like this: Notice that the line afterwards isn't quite flat: there's a hint of a damped low-frequency bounce.
Registered Member #1538
Joined: Thu Jun 12 2008, 07:28PM
Location: Bonn, Germany
Posts: 28
Thanks for the replies so far. The GDT is 6:12 turns, sorry, I shood have mentioned this. The core is about 5cm in diameter, well suited material (mat77 at reichelt, for those who know this surpplier).
The DC blocking cap is a 4,7uF Film type. And the driver ic's have a 100nF ceramic cap each and 100uF tantal (shared by to ic's) still very close.
I was not able to change the DC blocking cap back to an electrolytic one jet. I will try this, and also a GDT with more windings, later.
This site is powered by e107, which is released under the GNU GPL License. All work on this site, except where otherwise noted, is licensed under a Creative Commons Attribution-ShareAlike 2.5 License. By submitting any information to this site, you agree that anything submitted will be so licensed. Please read our Disclaimer and Policies page for information on your rights and responsibilities regarding this site.